Jeff sent me a picture update on how the repairs on the Triumph were going and things are looking good. I cannot wait to see the final results.
This blog follows my trials and errors in restoring a 1968 Triumph Spitfire, starting with a limited knowledge of cars. Hopefully, I'll be a pro by the end of this, or at least somewhat competent. ;-)
Friday, July 27, 2012
Monday, July 23, 2012
Chassis Update
Today I heard back from Jeff on the chassis and after coming back from sandblasting, they noticed 2 large rust holes and sizable dents on the outrigger part of the chassis.
Jeff offered services to straighten the bent mounts, cut out the rot, and fabricate new metal to patch the rust holes for $250, which I readily agreed to. I figured that I was already getting the powdercoating done and this would make things look that much better...I've just got to ignore the fact that this will cost more than what I paid for the original car.
Jeff offered services to straighten the bent mounts, cut out the rot, and fabricate new metal to patch the rust holes for $250, which I readily agreed to. I figured that I was already getting the powdercoating done and this would make things look that much better...I've just got to ignore the fact that this will cost more than what I paid for the original car.
Tuesday, July 17, 2012
Off to powdercoat
Chassis strapped to Chris' truck for transport
Leaving the chassis at Central MASS
Jeff also mentioned that if I emailed him a picture of any other car parts needing powdercoating, he'd send me a quote. Given that the already restored suspension parts (that I had taken the time to sand and spray paint) are already chipping from moving them around the basement, I am considering taking him up on the offer. At the same time, it feels like I'd be backtracking 2 years in my restoration effort to do this, but... long term, this would be the better thing to do. (1 step forward, 2 steps back...)
The chassis should be ready in 1 - 2 weeks, so I'll post an after picture as soon as I can.
Monday, July 2, 2012
Awesome Triumph Engine Rebuild
Had to share this youtube video that Chris had found... The video is comprised of 3000 pictures from an engine rebuild spanning 11 months!!
Great video...
Great video...
Sunday, July 1, 2012
Ready for sandblasting and powdercoating
Back in spring, I had found and emailed a powdercoating company nearby about powdercoating the Triumph chassis. Jeff at Central MASS Powder Coating in Clinton, MA emailed me back right away saying they could sandblast and powdercoat for ~$750. The chassis just needed to be fully disassembled and basically degreased before I drop it off. The shop would then sandblast, bake it out, mask all threads, and powdercoated with zink epoxy primer and then powdercoated with polyester taking about 1 week to do all this.
Then work became busy again and summer weekends started to fill up, so I did not get a chance to ready the chassis for sandblasting and powdercoating until this weekend. Despite the 90s temperature, the garage was bearable. Chris helped to pull out the differential which came out pretty smoothly. We used a jack to help support differential as the supporting bolts were removed and then a pry bar to dislodge the differential from the back mounts.
As for cleaning the chassis, I degreased years of dried, caked on grease with a can of degreaser, roll of paper towels, Q-tips (for those hard to reach places), and wire brushes. I had started a bit of this previously but today I spent about 3 hours getting everything scrubbed. At the end of all this, I was covered from head to toe with grease bits that looked like freckles on my skin and had a mess of paper towels, Q-tips, and grease bits on the plastic tarp I lined the garage floor with before starting.
Cleaning the chassis = the messiest I've been since this project started...
This used to be covered in grease...
Then work became busy again and summer weekends started to fill up, so I did not get a chance to ready the chassis for sandblasting and powdercoating until this weekend. Despite the 90s temperature, the garage was bearable. Chris helped to pull out the differential which came out pretty smoothly. We used a jack to help support differential as the supporting bolts were removed and then a pry bar to dislodge the differential from the back mounts.
As for cleaning the chassis, I degreased years of dried, caked on grease with a can of degreaser, roll of paper towels, Q-tips (for those hard to reach places), and wire brushes. I had started a bit of this previously but today I spent about 3 hours getting everything scrubbed. At the end of all this, I was covered from head to toe with grease bits that looked like freckles on my skin and had a mess of paper towels, Q-tips, and grease bits on the plastic tarp I lined the garage floor with before starting.
Cleaning the chassis = the messiest I've been since this project started...
This used to be covered in grease...
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